|Nov 10, 2013, 08:09 PM||#1|
Apple II Rebuild
Several years ago, I acquired a 1979 Apple II Europlus. It has mostly been a collectors item, stored carefully on a shelf and powered on from time to time to test its circuits. It had been shelved for upwards of 12 months now and was well overdue for a startup.
It started up perfectly fine, and I left it to idle while I looked up some documentation for it. About 15 minutes in, the machine made a strange noise which sounded like the Floppy Drive accessing, so I didn't think much of it.
A few seconds later, the machine made a POP sound, followed by a CRACK, and a huge amount of thick, acrid smoke started pouring out of the case. A sticky brown liquid started dripping out of the ventilation gaps in the lower casing and on to the desk.
With that, the machine was dead. It was 35 years old. Not a bad effort.
Part 1: Diagnosis
I removed the power supply, an ASTEC AA11042C from an Apple IIe that may have been fitted to the machine as a replacement in the 1980s. The PCB inside the supply is dated 1982, so the supply in itself is around 31 years old. When I lifted the covers... well, I'll let you see for yourself.
This large gold-coloured component, an EMI Suppression Capacitor, has cracked around several edges and thrown out a gold-brown coloured fluid. I suspect it's been leaking for some time, because after desoldering the component, I can see that it's pooled below the component in a sticky mess, even making its way through one of the unused holes in the PCB.
I cleaned the PSU with a mixture of a Throttle Body cleaner and Alcohol to dissolve and rinse away the sticky mess, going over component legs and traces with a cloth and brush to remove it. I didn't want to leave this stuff anywhere in the PSU as it has the potential to cause further damage if not attended to.
Many of the component's markings were destroyed when it failed, but I can see it's a Rifa 0.47uF 250V EMI Suppression Capacitor (X2 Type), used to filter the AC power coming in from the mains.
After some research, I can see these are notorious for failing in exactly the manner this one did with old age. This website was the most helpful, and the failure is well documented under the heading Line Suppression Capacitor. As you can see, when they fail, they do so in a rather spectacular manner.
Another nearby component looks to also be in the process of failing as a dark patch can be seen underneath it, suggesting it may be leaking and ultimately headed for the same fate.
This is one of the least favourite moments for any Apple or even vintage electronics collector. Watching your pride and joy go up in smoke is never a fun experience, but sometimes you can be fortunate. Thankfully this time is one such occasion. After a thorough cleaning and examination of the PCB, it appears that the board itself is in good shape, with no damage to any traces, solder joints or even surrounding components, and these older supplies are easy to service, with no surface mount components and widely spaced connections and tracks.
After researching the issue and consulting with some members of the Badcaps Forum, it looks like a replacement of the failed and failing EMI Suppression Capacitors along with a new fuse will bring this old power supply back to life. There are higher quality replacements for the Rifa brand components that aren't as susceptible to failure in this manner, which should aid in improving the reliability of the power supply when it's returned to service.
Part II: Repair
Swapped out the Rifa 250V 0.47 X and 0.1uF X2 capacitors for brand new Suntan 275V 0.47uF X2 and 0.1uF X2 Metallised Polypropylene capacitors. They're not the best supplier but definitely functional. The existing components had extremely messy solder joints, which were cleaned up, and one of the traces on the underside of the board needed adhering back to the PCB.
Overall though, the repair went extremely well.
Now, this machine smelled like the inside of a International Roast tin. That capacitor residue smelled like coffee, but not in that pleasant way. The smell persisted after replacing the Line Filters in the power supply, so I decided to tear the machine down and service it, and try to find the source of the smell while I was at it.
It didn't take long. It made a nice outline of the power supply. Also, check out that perished speaker foam. It was like powder.
I stripped the machine down to the bottom pan and scrubbed it down with solvents and cleaners. A few seconds in the solvent and the stuff washed off like water. I sprayed the underside of the Logic Board and around the connectors and chip sockets with circuit board cleaner, but it'll take some scrubbing to remove that caked-on dust around the slots and components.
I removed the speaker foam and replaced it with a single double-sided adhesive foam disc, stuck to the lower pan. Holds in place with no problems.
I did take the keyboard apart and give that a clean out as well, but I didn't take any pictures of that process. Needless to say keyboards are my least favourite part of any computer service. After that was done, the machine was reassembled and powered up for testing.
Impressively, the video quality has improved quite a bit. No more faint vertical lines on the display, only a perfectly crystal-clear image. You try taking a picture of an awful, low quality Twisted Nematic display though.
Interestingly, it also looks like the machine has been modified. One chip has been removed, a chip socket has been stacked on top of the existing chip socket, but with two red and black wires coming off it. Then the existing chip has been stacked on top in a piggyback configuration. The two wires travel up to the keyboard connector, with the black connecting to the second pin from the left, and the red connecting to the third pin from the right (looking directly at the connector from the back of the machine, not the front).
I have no idea what these do, but the keyboard works fine with them disconnected, so I suspect it's a modification of some sort rather than a fix.
Anyway, with only the memory expansion card fitted, it seems to be running fine and it isn't pushing the PSU too hard. Overall, it's a much happier machine.
Part III: Rebuilding the Disk II
Satisfied that the PSU is in working condition, I refitted the Disk II controller card and hooked up the 5.25" disk drive. It had no issues with writing a ProDOS disk using ADTPro over the cassette interface, but reading that disk back proved difficult. The drive was also unable to write to my Verbatim and MagMedia brand disks.
Not satisfied that I was dealing with a bunch of defective disks, I turned my attention to the drive.
This drive lacks any kind of external markings, so after opening it up, I was surprised to see it's in fact a standard Shugart SA390 mechanism. The motors are of rather decent quality, the stepper motor in particular is an American made motor built by North American Philips Controls Corp. in Cheshire, Connecticut.
I thought I was dealing with a healthy drive. I may have overestimated the reliability of a drive mechanism now over 30 years old. The tracks were rough and in need of cleaning and polishing, the heads were dirty and the drive belt was slipping around the smaller pulley.
First things first - I had to strip it.
But I didn't get any photos of this process.
I started by removing the collet hub and upper structure that lowers down when the drive door is closed. Then the head assembly and tracks came off. The large brown disc with the track cut into it is press-fitted and had to be hammered off the centre hub, and the stepper motor was removed. The drive belt was removed, and the motor that drives the belt was removed.
Everything was sprayed down with solvent and scrubbed clean. Then, into the oil it went! The moving parts were brushed down with a thin coating of Shell Helix 20w50 engine oil, and using a syringe, some oil was injected into both of the electric motors. The top section of the drive was reassembled, including the collet hub, upper structure, tracks, head assembly, spindle motor and the stepper motor. The brown tracking disc was pressed back onto the hub, and the drive was powered up to check movement.
Success! Full range of motion in the head assembly.
Turning my attention to the belt, I noticed it's a slightly rubbery, interwoven fabric material and is actually quite durable. The belt was soaked in a silicone-based belt dressing then wiped down to remove any excess. The belt was slipped back over the spindle pulley, then over the spindle motor pulley. I pulled the motor out as far as it would go and tightened the screws to tension the belt.
No more slipping!
Afterwards, it was simply a case of starting up the machine, loading across a copy of Apple-Cillin and running a drive speed test. The motor was running a little on the fast side by a few revolutions. A Disk II motor needs to run as close to 300rpm as possible, but the drive works reliably if the RPMs are clocked a few revolutions slower. Running it faster is when issues start to occur. After winding the motor down to around a steady 295-297, all that was needed was to swap in a blank disk, format it, write to it and boot from it.
Impressively, this seems to have done the trick. The Verbatim and MagMedia disks are now capable of reading, it can write a copy of ProDOS down with ease and boot from it in just a few seconds flat.
I closed up the drive assembly and finished it off with a set of 4 brand new rubber feet.
Having this disk drive functioning again makes transferring data to the Apple II significantly easier. Before the drive worked, I would have to boot up over the cassette interface and load data into memory, which does take quite a while. Starting up from the drive takes only a few seconds.
Part IV: Repairing the Joystick
Now that I have some software on the system, I would like to do something with it. So I hooked up the Joystick, loaded a game and... nothing. The keyboard input worked fine, but attempting to use the paddle buttons had no effect on the Apple II.
Here we go again.
This Joystick could have been a brand name unit at some point, but its labels have since been peeled away, so I don't know much about it. The buttons have a nice feel to them, and the Joystick assembly has a nice amount of spring tension. It's not perfect, but it's more than adequate for playing games with.
Inside is a mess of wires and components, but nothing out of the ordinary for other electronics of the era. I'm almost positive that this Joystick has been worked on before, as it has some telltale signs of damage where a track has been pulled off the board and some wires have been cut and taped back together. One wire was completely loose inside the case, explaining why the buttons wouldn't fire.
I took the button out and ran two new wires down the stem of the Joystick, soldering them in place of the old, frayed and cut wiring. One solder track on the PCB was lifted and missing entirely, which was fixed by soldering a small piece of wire in place of the old track. The Green wire was rather in rather good condition, but broken up near the PCB, so I trimmed it back a little and resoldered it.
All it needed then was a quick clean up.
Best of all, I was able to play a few rounds of Pitstop II with it. Looks like the repairs paid off.
Now if only I wasn't so terrible at that game.
Part V: Finale
This Apple II was owned by someone that clearly loved it. When it came to me, it was carefully boxed in the original shipping container, with all foam pieces intact. The container itself wasn't as fortunate, stained with water and torn, but they had definitely made an effort to look after it, both in use and in long term storage.
Even so, a machine of its age doesn't come away completely clean. The case is textured with many high and low points in the plastic, and over the years dirt accumulates in the surface. I've tried removing this dirt with alcohol and some light dishwashing liquid, but I needed something with a little more kick for this job.
After seeing the various marks and patches on the walls and paintwork of the house vanish like magic with this stuff, I decided to give Selley's Sugar Soap a whirl. For reference, I used it diluted in water, and tested on a spare Macintosh Classic case I had around first, where it worked a treat. On to the Apple II!
I went over the case in concentrated areas at a time, focusing on the top, sides, keyboard surround, base plate and back panel individually. It didn't take much effort, and a microfiber cloth and the Sugar Soap in a spray bottle was all that was needed. Spraying it on to the plastics directly and buffing with the cloth was enough to bring the finish up nicely. For the more difficult areas, such as the keyboard and rear panel, I sprayed it onto the cloth instead of the case.
I had to take care while cleaning around the badge and the label on the base of the machine. The badge is in rather good condition, but the dirt had settled into the seam where it meets the case.
It wasn't long before the machine was back to looking like a showroom display model. The shade of the plastic is exactly as it was 34 years ago. Not a hint of yellowing anywhere on it. While photos are often forgiving to minor imperfections, I can honestly say that the pictures are a rather accurate reflection of the machine. The plastics are absolutely perfect.
The total cost of the repair was $21.70 in tools and components. Additional tools, such as soldering irons, screwdrivers, detergents, oils, microfiber cloths and brushes were already in my possession and haven't been added to the total. It took about 18 hours at 4.5 hours a day for 4 days to complete the build, although it could be completed much sooner if you were to dedicate yourself to it with no distractions.
Using ADTPro to transfer data to and from the Apple II via the Cassette Interface is an exercise in patience, but it is a cheap and effective method of transferring data from a MacBook Pro to the Apple II. Using this method, the Apple II now runs ProDOS 1.9.
While the Apple II has now been returned to its display cabinet, I'm sure it will still be started up from time to time. It's a valuable piece of computing history, and with the work it has received in this past week, it will continue to function and be usable to myself and any future owners for quite some time.
Yet another project completed. Until next time, the next project, whatever it may be.
Apple Certified Macintosh Technician (ACMT)
Developer, LeopardAssist - Install OS X Leopard on some unsupported Macs.
Administrator, ThinkClassic - A Vintage Apple computer community.
Last edited by iMacC2D; Nov 10, 2013 at 08:29 PM.
|Nov 10, 2013, 09:45 PM||#2|
You did a dang good job cleaning this up, handled like a master repairman! Blown caps seem to be a high cause of failure in older electronics, unfortunately.
As for the modification in the computer, isn't the 558 chip a quad timer chip? Don't know why it would've been replaced/modified but this was the age of CMOS and finicky-ness. Perhaps one stopped working a while ago, or it was the equivalent of a "green wire" fix? Either way it's an odd addition.
On a side note, what soldering iron(s) do you have? I'm about to upgrade and am looking for good reviews from real people who have more experience than I do.
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|Nov 10, 2013, 11:19 PM||#3|
Excellent post and a great write-up.
The two clips are most likely a keyboard shift-key mod. It uses the game port button to emulate (via software) an upper case key stroke. Usually used on 80 column cards. Normally done as a single wire mod, I can't remember why the addition of the second wire, unless it's actually for left & right shift keys.
iBook14" 1.42Ghz, G4 DigitalAudio 733Mhz, iMac Snow 700Mhz, iBook SE 466Mhz, PowerBook Pismo 500Mhz, G3 B&W, G4 MDD 1.25Ghz, iMac 233 1998, iMac G4 USB2 1.25Ghz, iMac C2D 2.16Ghz, MacMini G4 1.25Ghz
|Nov 11, 2013, 06:28 AM||#4|
Thanks! Capacitors are one of those major failure points in older electronics. Sometimes the failure is rather forgiving and the power supply simply won't start up, other times it can be rather awful and messy, like it was in this case.
I'm not exactly a professional myself, I studied Electronics in Grade 11 (2008) and Electrotechnology in Grade 12 (2009). I immediately went to Apple and became a Certified Technician, so component-level repairs were never something I did that frequently. I'm only 22 mind you, so hopefully there's plenty of time to learn a little more and continue working on these skills.
I bought a rather cheap 20/130W Turbo Soldering Iron for $18.00 as a temporary measure when my old iron burned out, expecting to only get around 6 months out of it, but so far it's continued working perfectly. I hear the Turbo button can damage the iron or wear it out prematurely when used frequently, so I've stayed away from it.
Of course you can get much, much better irons if you're willing to spend a little more. I'd always recommend a proper temperature controlled iron if you're willing to do serious soldering. Not that it's impossible to use a cheap iron, but it does take a little more effort and it can be difficult to get a professional result sometimes.
MacTech68: I think you could be on to something there. I've always noticed the behaviour of the Shift Keys to be consistent with the behaviour outlined in that Apple support article. I'll have to disconnect the wires at some point and see if the behaviour changes to be sure, but it would make sense, especially since it sounds like it was fairly common for the era.
|Nov 11, 2013, 09:17 AM||#5|
I'm not sure what programs/OS took advantage of this mod, but most were word-processors and more advanced OS' like CPM (requiring a Z80 CPU Card and 80 Column Card). Many of the 80 Column cards for Apple II (NOT APPLE IIe) came with this mod kit.
EDIT: also, just a tip - if the PSU shuts down when more load is added (additional drives, more cards) replace the cap circled in red below.
iBook14" 1.42Ghz, G4 DigitalAudio 733Mhz, iMac Snow 700Mhz, iBook SE 466Mhz, PowerBook Pismo 500Mhz, G3 B&W, G4 MDD 1.25Ghz, iMac 233 1998, iMac G4 USB2 1.25Ghz, iMac C2D 2.16Ghz, MacMini G4 1.25Ghz
Last edited by MacTech68; Nov 11, 2013 at 09:29 AM.
|Jan 19, 2014, 06:37 PM||#8|
Very useful. The exact same component in my IIe PSU has just popped , you're right, the smell is horrendous.
Going to be taking it to pieces tomorrow and begin de soldering that component. Hopefully I can find a replacement easily.
|Jan 19, 2014, 08:12 PM||#9|
Very nicely done!
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|Mar 2, 2014, 06:28 PM||#11|
I liked, and adopted the expression.
For soldering tools, Hakko, and Weller are my choice: I had a brill Weller SMD station back in the 1990s, and I loved it to death. Even the inexpensive Weller, and Hakko tools are of reasonable quality. Some outfitters sell one or the other with a very-fine end, and the other brand with a normal to fine end, for between £10 and £20.
My tip: Buy a basic thermal station, with an analogue thermostat/rheostat, and ignore whatever tool comes with it. Then, buy a decent Weller, or Hakko pencil, and use it through the station: The thermal stations aren't all that different by brand, unless you want digital controls. In that case, buy a station from Weller, with hot air, and suction.
Regarding component-level repairs: That used to be required to become an authorised Apple serviceman. After the SE-era, Apple changed to the 'replace the mainboard' policy, but repairs used to be done on-site. I retainted this philosophy through to 2006, which is when I stopped doing Apple service, as I didn't want to deal with Intel systems, for component level repair was next-to-impossible on them.
Everything by then was a BGA, which is not a fun component to reflow.
Last edited by AmestrisXServe; Mar 2, 2014 at 06:35 PM.
|Mar 3, 2014, 12:47 AM||#12|
In the height of the Apple II era, while it wasn't an Apple II .. it was actually an Atari Time 2000 pinball game. It was outside a friends house, he'd just gotten it and it was acting funny, which was typically normal for Atari pinball machines.
On a pinball machine, the glass slides out the front and the play field raises up like the hood on a car, and you prop it with a stick.
Typically of the era, there were large power supplies in the bottom, and electronics in the head unit.
So I'm leaning in from the side trying to get readings on a lantern battery sized capacitor and a nearby bridge rectifier. The thing was dimming and coming back on a bit more rapidly than it should be and occasionally resetting the CPU.
I was in the wrong place .. at the right time ;-)
Another of those giant sized capacitors just blew it's top off. In this case, these things are mounted with the terminals facing up, and have screw posts rather than leads like PCB mounted units.
I kinda reacted just in time because as I was standing there I started to hear a hissing sound and then turned to see smoke starting to come from around the edge of a screw terminal before it went off. In the instant that I moved up and back, it went off and my head hit the play field as I was backing out, all I remember was a really low frequency reverberating pop, and white everywhere. As I went backwards and nearly tripped over stuff, after I'm about 15 feet away I can see surroundings again. The play field had slammed down and the whoosh created a gap in the smoke column and it had the appearance of a mushroom cloud. As I realized what had happened I screamed "holy ... " you can guess the other two words.
Then it started raining bits of white fine paper stuff, only slightly sticky.
I screamed 'nuclear winter!' and.. and his younger sister came out of the house, oblivious to all the smoke, barking dogs, and 'snowing paper crud' .. "Next time use less expressive language!" ..
Yup. Capacitors, have an amazing capacity. ;-)
|Mar 10, 2014, 11:48 AM||#13|
I've often thought about purchasing better soldering equipment, especially after attempt to desolder capacitors from a 2006 iMac last week, which of course uses lead free solder. My little $25 iron couldn't hack it. The problem is that I'm a student again (Yay...) and I can't afford to spend hundreds in replacing this equipment at this stage.
Of course I have a MacBook Pro Logic Board repair coming up that will require a higher wattage iron... not looking forward to that. I do have a variable temperature iron that isn't currently working, so I'll perhaps look at the power supply and see if I can repair that one.
I still perform component level repairs on some machines, but I will agree that the Intel boards have become much harder to work with. Not impossible, but I still haven't gone too far into the Intel boards since I think I'd end up with more dead boards than working machines at this stage.
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